GX CS4-i First time turning on

My pump arrived Monday the 14th a day earlier than tracking initially showed. After reading numerous threads about first start up I decided I wanted an hour meter on mine. Also wanted to feed it from a nitrogen tank. The hour meter arrived Wednesday and was installed that evening. The fittings for converting to a nitrogen feed arrived 8:30 PM yesterday and were installed this afternoon. I need a hose barb fitting for my nitrogen regulator and will pick that up tomorrow at HD hopefully.

Filled the water reservoir with Dexcool 50/50 because that is what I had on hand. Ran the pump to check for leaks and purge any air out of the cooling system. Hooked up the supplied hose with the deadhead installed. Opened the bleed valve and turned the pump on. Watching the pressure gauge with anticipation and nothing. Oh no, I hope I did not break something doing the mods. Then it dawns on me, close the bleed valve. Whew, was that close to ruining a Friday afternoon in the shop.

So far it looks real good. 32~34 seconds to fill the line to 400 bar with the deadhead installed.

I bought an analog hour meter rather than digital just because. The hour meter would not fit on the front panel but would fit in the top or back. I chose the back only so I would not have to unplug wires to remove the case. The air filter hooked up to the bulkhead barb fitting will be replaced with a nitrogen feed tube when I get the regulator fitting needed.

How much do you guys fill the water reservoir? With no expansion tank like a car has on its cooling system there should be some space left when filling? How will I know if the cooling system water pump fails?

Thinking I would like to add a digital thermometer with a settable alarm if such a device exists in a panel mount package. Suggestions?

Pump 2.jpg


Pump 1.jpg
 
Nice work, how did you wire the analog hour meter?

would love to see the nitrogen set up once complete

Did you rotate the cooling fan as discussed in previous threads? there was some talk about the factory changing that after seeing the thread on this forum , seemed to be more efficient and kept the water cooler?

Did you order on amazon or from GX?

thanks for posting.
 
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I fill mine to just above the recirculation outlet. That leaves a bit of air space at the fill cap. I can still see flow through the cap, no need for LEDs for me. These don't run that hot so I don't see a need for a lot of expansion room. Make sure you work the bubbles out of the system (tilt it while running). I did rotate my radiator.
 
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Nice work, how did you wire the analog hour meter?

would love to see the nitrogen set up once complete

Did you rotate the cooling fan as discussed in previous threads? there was some talk about the factory changing that after seeing the thread on this forum , seemed to be more efficient and kept the water cooler?

Did you order on amazon or from GX?

thanks for posting.
If you look at my side view picture you can see two yellow dots. Those are the female half of the bullet connectors the factory uses to connect to 12v power to the pump motor. The crimp ends of the bullet connectors were not big enough for my hour meter wire and the factory wire. So I split the male ends open and soldered my hour meter wires. Then covered all with heat shrink tube long enough to cover the bullets when reconnected. Wired as I did it the hour meter will run only when the pump is running.

I have missed the fan rotation thread. Did not know anything about that. What is it? Reversing the air flow?

I ordered direct from GX and saved about $100 over the Amazon price.
 
I fill mine to just above the recirculation outlet. That leaves a bit of air space at the fill cap. I can still see flow through the cap, no need for LEDs for me. These don't run that hot so I don't see a need for a lot of expansion room. Make sure you work the bubbles out of the system (tilt it while running). I did rotate my radiator.
That was how I guessed and filled mine. I also removed the aluminum cross under the water tank glass cap. I can now easily see the water moving. I believe I got mine bubble free but will go out and tilt it a bit to make sure.
 
Here is something else that my interest those doing an hour meter on the back panel.

To make the cutouts in the back panel I wanted to use my drill press to remove as much material as I could to minimize the hand file work. This required the pump be face down on the drill press table. I used a 2X piece of construction grade southern yellow pine. Laid out the outline of the pump front panel so the cutout was 1/2" less on all sides than the face of the pump panel. This allowed the pump to lay face down with nothing touching the cast iron drill press table. I also placed an old towel over the wood so I would not scratch the nice shiny paint job.

Of course all the pump internals were covered with shop rags to keep metal chips and shavings away.

Pump 3.jpg
 
If you look at my side view picture you can see two yellow dots. Those are the female half of the bullet connectors the factory uses to connect to 12v power to the pump motor. The crimp ends of the bullet connectors were not big enough for my hour meter wire and the factory wire. So I split the male ends open and soldered my hour meter wires. Then covered all with heat shrink tube long enough to cover the bullets when reconnected. Wired as I did it the hour meter will run only when the pump is running.

I have missed the fan rotation thread. Did not know anything about that. What is it? Reversing the air flow?

I ordered direct from GX and saved about $100 over the Amazon price.
did not reverse the air flow but the two water outlets are now on the side as opposed to the bottom
 
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I fill mine to just above the recirculation outlet. That leaves a bit of air space at the fill cap. I can still see flow through the cap, no need for LEDs for me. These don't run that hot so I don't see a need for a lot of expansion room. Make sure you work the bubbles out of the system (tilt it while running). I did rotate my radiator.
Does it matter which way you tilt the machine in relation to the radiator or inlet/outlet hose placement?
 
Does it matter which way you tilt the machine in relation to the radiator or inlet/outlet hose placement?
I tilted it while running to the front, like 1900colt posted in this forum, and it got out a lot of air. Later GX had me run the water pump and tilt it left and right 90 degrees as part of a troubleshooting procedure, but I didn't notice any more air purging, but that s was after I rotated my radiator. Rotating the radiator mounting gets some more out after you do the mod.
 
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I think he said it didn't matter which tube went to which port as the cooling was the same. You could follow up on his thread/post . assume you saw the pictures.
If the radiator is not rotated, you want to tilt to get the outlet side higher. The video I made shows it running with the cover off and if you look close, as soon as the compressor is tilted, air starts to escape.

If rotated, I prefer the outlet hose to be on top, as that will clear the air pocket naturally and a slight tilt to make that outlet the high side for a minute will be even more effective at clearing any trapped air.
 
Put my GX CS4-i to real use for the first time today to fill the 480 CC bottle on my Ghost. Starting pressure was about 80 bar on the Ghost gauge. GX pump gauge turned off the compressor at 250 bar and the Ghost gauge read 240 bar. After the Ghost tank cooled to room temperature the Ghost gauge read about 225 bar. Total pumping time was 8:31. The pump coolant temperature reached a max of 93.5 degrees fahrenheit in an air conditioned shop. Note that I have not done the radiator rotate mod. I also did not use nitrogen today although I have the setup ready to use but have not tested it.

A real temperature test will be this summer using the compressor outside in our 95 degree temps.
 
Just received my cs4. Something to note that I learned right off the bat. First use was going to be a top off of a 6.8L. I let it run til the gauge on the cs4 was about 3500 psi as there was 3k in the scba. Then I opened the valve on the tank. The cs4 immediately stopped. The next try even though the cs4 line pressure was above the tank pressure I opened the tank valve very slowly easing a little at a time. No problem at all when I did it that way. Been going like 45 minutes and I’m just a touch over 4k. Open your tanks slowly as to not overwhelm the machine.