Hi, I rebuilt my Impact M3 2nd regulator using bras piston. But after reassembly it leaks quite heavily (hissing).
What could I have done wrong?
What could I have done wrong?
Hi, I rebuilt my Impact M3 2nd regulator using bras piston. But after reassembly it leaks quite heavily (hissing).
What could I have done wrong?
This is the post of the year so far...I'm going to have to work hard to out-do this one for next year!Probably messed up the rebuild.
Doesn't have to be wordy to be accurate. There's 6 orings there, one probably isn't sealing. Easy troubleshootingThis is the post of the year so far...I'm going to have to work hard to out-do this one for next year!
I probably didn't allow for enough gap when re-assembling. I did't notice it but GC did that it's longer than stock.Or O ring X2-8 never got replaced. Not replacing that is a 75/25 ordeal, with 75% leaning towards a leak and if your one of the lucky 25% that don’t get a leak.
That’s too bad about your experience, Jimmy. I’ve installed these brass pistons on three impacts and they’ve all done well
Yeah wouldn't even fill the plenum with the fx brass one. Several MM longer than the stock delrin one. Why they changed the material AND dimensions baffles me.I probably didn't allow for enough gap when re-assembling. I did't notice it but GC did that it's longer than stock.
It looks like the outer boreWhere is it leaking from, the adjuster screw or the outer bore ?
I am afraid it is X2-8. I did change it. But it was really difficult to get it out, so I could have scratched the body. It looks like it leaks not through adjuster screw, but the outer bore. Not easy to tell because air is hissing heavily. I wonder if there is any way to prove that this is exact reason, and if that means that now I have to change the whole trigger block ?My guess is the X2-5 o-ring got nicked by the brass piston
View attachment 314116
View attachment 314117
Can you not place a little soapy water on just the adjust screw and its threads and then the outer set of threads. Eye dropper works well.I am afraid it is X2-8. I did change it. But it was really difficult to get it out, so I could have scratched the body. It looks like it leaks not through adjuster screw, but the outer bore. Not easy to tell because air is hissing heavily. I wonder if there is any way to prove that this is exact reason, and if that means that now I have to change the whole trigger block ?
Yessir, that looks more like it. I like that larger surface area. Did you slightly dome the peek seat?View attachment 314210
My brass pistons work great for me.